It was very encouraging to note that the model predicted the
evaporator air outlet temperature very accurately to within an error
of 2%. This established the accuracy and the validity of the model,
which now could be used to predict performance of a blast freezer
as well as a design tool for future blast freezers in order to achieve
higher energy efficiency.
12. Design improvements
Odey
[47]
investigated performance enhancing measures of
a batch air blast freezer. He found that generalised rules of thumb
have been used for the design of air flow through blast freezers.
Critical aspects of the design and implementation of the airflow
circuit are often excluded from the refrigeration contract, resulting
in poorly implemented and underperforming facilities. Typically,
the refrigeration contractor’s response to poor freezer perfor-
mance is to increase the fan capacity and power. It was found that
simply increasing the air flow by increasing fan speed did not
necessarily increase the air speed through the cartons in the
freezer. The higher fan speed resulted in negative velocities at the
fan inlet due to the formation of a large unstable vortex. As a result
more heat was added to the freezer from the fans thus reducing
the efficiency.
The following modifications were installed on the air blast
freezer:
Baf
fling on the top and sides of the freezing chamber
Fan inlet cone and diffuser
Air inlet and discharge vanes on corners
Variable speed drive on fan
Prior to the modifications the air flow entering the fan was
highly unstable with significant flow reversal. This turbulence
reduced significantly with the above modifications. Most of the
pressure drop in the unmodified freezer occurred at the 90
turning
points, whereas the modified freezer had the largest pressure drop
through the product pallets. As a result of the experiment, the
existing 11 kW fan motors drawing 8.7 kW were replaced with
Fig. 8.
System model flow diagram.
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